* Output from Troll field reduced by 30 mcm/d
* Kollsnes gas processing plant
(Adds Statoil, power outage, analyst, gas flows)
OSLO, Oct 12 (Reuters) - Output from Statoil'sTroll natural gas field offshore Norway has been reduced due tosafety issues, gas system operator Gassco said on Friday,raising concern about supply safety after a string of outages.
The shutdown comes after a series of supply disruptions atNorway's key gas processing plants over the last two weeks,which pushed UK gas prices higher and left traders worried aboutstability of deliveries in the upcoming winter.
The 145 mcm capacity Kollsnes gas plant that processes gasfrom Troll for export to Britain and Europe reported powerconsumption dropped to 50 MW from 270 MW, indicating a sharpreduction in production.
A Statoil spokesman declined to comment.
A spokeswoman for Norway's Petroleum Safety Authority saidthe watchdog not notified about any safety issues.
Companies have to inform the safety authority only aboutmajor incidents, she added.
Still, the outage is going to boost market anxiety.
"The volatility of Norwegian gas flows to the UK duringrecent weeks is a source of concern," Dragos Talvescu, anOslo-based analyst at consultancy Sund Energy, said.
"If that happens during winter time, there could be panicand large spikes in the UK prices," he added.
The Gassco-operated Kollsnes plant also processes gas fromthe Kvitebjoern, Visund and Fram fields.
Gas flows from Norway at 1100 GMT were not affected, datafrom Gassco showed. The Langeled pipeline, UK's main subsea gasimport route fed by the Nyhamna processing plant, was pumping70.8 mcm of gas per day.
Outages in production are not immediately reflected in theflows because there are large gas volumes in the pipelines.
(Reporting by Nerijus Adomaitis; editing by Balazs Koranyi andKeiron Henderson)
Keywords: NORWAY KOLLSNES/